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Turbine Traveller

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Aircraft Technician based in Nairobi| Avgeek |Sharing industry trends & breaking aviation news |Enlightening the skies| Reach out @[email protected]

Shorts

Here's the full surveillance video showing moments before the Lufthansa Boeing 787-9 (D-ABPQ) nose gear collapsed at Frankfurt. If you watch closely, the nose landing gear doors open first, indicating what appears to be the start of a normal landing gear retraction sequence. According to reports, the Dreamliner had logged a maintenance request the previous day involving a landing gear door error message. On the Boeing 787, maintenance personnel can place the aircraft into a special maintenance mode (on the overhead panel, turn switch to "enable"). Boeing manuals emphasize that if maintenance mode is enabled, hydraulics are powered, and the gear lever is selected UP, the landing gear can retract regardless of weight-on-wheels protection. To prevent this, there's an override button where the gear handle lockout can be bypassed to move the gear handle even if it is locked out. The only way this can happen is by intentionally bypassing the normal safety lockouts used during maintenance procedures. Outside of maintenance or certain emergency procedures, the aircraft's weight-on-wheels system prevents gear retraction on the ground. Lufthansa says the aircraft has since been recovered. Fuel was removed, the jet was lifted, the nose gear was re-extended, and the aircraft was successfully towed under its own weight to a maintenance hangar. Germany's Federal Bureau of Aircraft Accident Investigation has completed evidence collection from the aircraft and is now gathering witness statements. An interim report is expected within approximately 8 weeks. 📹: airlinersde via YouTube, link on first comment here.

Here's the full surveillance video showing moments before the Lufthansa Boeing 787-9 (D-ABPQ) nose gear collapsed at Frankfurt. If you watch closely, the nose landing gear doors open first, indicating what appears to be the start of a normal landing gear retraction sequence. According to reports, the Dreamliner had logged a maintenance request the previous day involving a landing gear door error message. On the Boeing 787, maintenance personnel can place the aircraft into a special maintenance mode (on the overhead panel, turn switch to "enable"). Boeing manuals emphasize that if maintenance mode is enabled, hydraulics are powered, and the gear lever is selected UP, the landing gear can retract regardless of weight-on-wheels protection. To prevent this, there's an override button where the gear handle lockout can be bypassed to move the gear handle even if it is locked out. The only way this can happen is by intentionally bypassing the normal safety lockouts used during maintenance procedures. Outside of maintenance or certain emergency procedures, the aircraft's weight-on-wheels system prevents gear retraction on the ground. Lufthansa says the aircraft has since been recovered. Fuel was removed, the jet was lifted, the nose gear was re-extended, and the aircraft was successfully towed under its own weight to a maintenance hangar. Germany's Federal Bureau of Aircraft Accident Investigation has completed evidence collection from the aircraft and is now gathering witness statements. An interim report is expected within approximately 8 weeks. 📹: airlinersde via YouTube, link on first comment here.

231,418 просмотров

WATCH: A Lufthansa Boeing 787-9 Dreamliner (D-ABPQ) sustained substantial damage after its nose landing gear collapsed while parked at the gate at Frankfurt Airport. The incident led to the cancellation of today's LH450 to LAX service as airport and airline teams assess the extent of the damage. Video from the scene shows the aircraft resting on its nose after the front landing gear unexpectedly gave way while stationary. No injuries have been reported, but a technical investigation into the cause of the collapse has been opened.

WATCH: A Lufthansa Boeing 787-9 Dreamliner (D-ABPQ) sustained substantial damage after its nose landing gear collapsed while parked at the gate at Frankfurt Airport. The incident led to the cancellation of today's LH450 to LAX service as airport and airline teams assess the extent of the damage. Video from the scene shows the aircraft resting on its nose after the front landing gear unexpectedly gave way while stationary. No injuries have been reported, but a technical investigation into the cause of the collapse has been opened.

1,637,472 просмотров

A passenger aboard Iberia A350 flight for Madrid recorded the moment a fire truck snozzle offering a water salute clipped the left wing of the aircraft. So unfortunate—a celebratory flight canceled, leaving them stuck in Ecuador.

A passenger aboard Iberia A350 flight for Madrid recorded the moment a fire truck snozzle offering a water salute clipped the left wing of the aircraft. So unfortunate—a celebratory flight canceled, leaving them stuck in Ecuador.

787,418 просмотров

The winds are strong enough to lift a parked Boeing 747.

The winds are strong enough to lift a parked Boeing 747.

1,104,371 просмотров

The mighty Atlas A400M threading its way through the Welsh Valleys. 📹: bards_eyeview

The mighty Atlas A400M threading its way through the Welsh Valleys. 📹: bards_eyeview

70,792 просмотров

Lead plane marking the drop spot for a DC-10!

Lead plane marking the drop spot for a DC-10!

1,164,912 просмотров

At LaGuardia Airport, New York Tower ATC: "I messed up." Another pilot: "Nah, man, you did the best you could."

At LaGuardia Airport, New York Tower ATC: "I messed up." Another pilot: "Nah, man, you did the best you could."

6,883,216 просмотров

Indian investigators are set to visit Seattle for Boeing lab testing tied to the Air India Flight 132 incident involving Boeing 787-8 VT-ANX. The aircraft, operating London Heathrow–Bengaluru on Feb. 2, 2026, was grounded after pilots reported the left Fuel Control Switch slipped from “RUN” to “CUTOFF.” Officials want Boeing to prove under controlled testing that the fuel switches cannot move on their own — even under vibration, turbulence, electrical faults, or other extreme conditions. Boeing is expected to demonstrate that the switch will not move unless physically operated by a human. The outcome of the tests could play a major role in determining whether the incident was caused by mechanical failure, external factors, or human interaction.

Indian investigators are set to visit Seattle for Boeing lab testing tied to the Air India Flight 132 incident involving Boeing 787-8 VT-ANX. The aircraft, operating London Heathrow–Bengaluru on Feb. 2, 2026, was grounded after pilots reported the left Fuel Control Switch slipped from “RUN” to “CUTOFF.” Officials want Boeing to prove under controlled testing that the fuel switches cannot move on their own — even under vibration, turbulence, electrical faults, or other extreme conditions. Boeing is expected to demonstrate that the switch will not move unless physically operated by a human. The outcome of the tests could play a major role in determining whether the incident was caused by mechanical failure, external factors, or human interaction.

909,153 просмотров

A flight attendant was found outside the Air Canada Express CRJ-900 by Port Authority Police, still strapped into her jumpseat, due to the catastrophic destruction of the forward section where crew are positioned.

A flight attendant was found outside the Air Canada Express CRJ-900 by Port Authority Police, still strapped into her jumpseat, due to the catastrophic destruction of the forward section where crew are positioned.

4,690,221 просмотров

This is a perfect video from Air Tractor inside the hangar showing how flight control surfaces respond when the right conditions are met. Ailerons control roll, the elevator controls pitch, and the rudder controls yaw.

This is a perfect video from Air Tractor inside the hangar showing how flight control surfaces respond when the right conditions are met. Ailerons control roll, the elevator controls pitch, and the rudder controls yaw.

293,923 просмотров

WATCH: Newly released airport surveillance footage of UPS Flight 2976 shows the exact moment the MD-11F's left engine and pylon separated from the wing just seconds after liftoff from Louisville back on Nov. 4, 2025.

WATCH: Newly released airport surveillance footage of UPS Flight 2976 shows the exact moment the MD-11F's left engine and pylon separated from the wing just seconds after liftoff from Louisville back on Nov. 4, 2025.

515,359 просмотров

Who did this now?

Who did this now?

846,517 просмотров

Here’s how you deliver a document to a pilot when the doors are already closed for departure. The pilot said thank you—with a candy 🍬✈️

Here’s how you deliver a document to a pilot when the doors are already closed for departure. The pilot said thank you—with a candy 🍬✈️

5,191,289 просмотров

DC-10 American Airlines flight 191's May 1979 accident at Chicago O'Hare and UPS MD-11 flight 2976's crash in Kentucky November 2025 had one major similarity: engine 1 separated during takeoff.

DC-10 American Airlines flight 191's May 1979 accident at Chicago O'Hare and UPS MD-11 flight 2976's crash in Kentucky November 2025 had one major similarity: engine 1 separated during takeoff.

197,120 просмотров

Pilots must notify maintenance when there's a hard landing and write a safety report about the incident. 📹: Dutchspotter

Pilots must notify maintenance when there's a hard landing and write a safety report about the incident. 📹: Dutchspotter

203,680 просмотров

This Kuwait Airways Boeing 777-300ER seems to have entered a near-stall condition following an excessive flare during landing at Schiphol Amsterdam Airport.

This Kuwait Airways Boeing 777-300ER seems to have entered a near-stall condition following an excessive flare during landing at Schiphol Amsterdam Airport.

5,537,137 просмотров

Jay Leno popping out of the nose of a Grumman HU-16 Albatross while it flew over the Pacific Ocean.

Jay Leno popping out of the nose of a Grumman HU-16 Albatross while it flew over the Pacific Ocean.

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Enjoy the thrust reduction sound of this massive KLM Boeing 777-300. 📹: Aviationmadness

Enjoy the thrust reduction sound of this massive KLM Boeing 777-300. 📹: Aviationmadness

134,826 просмотров

WATCH: Lightning and turbulence as a Boeing 777 flew over Taiwan through Typhoon Podul last night. The aircraft landed safely.

WATCH: Lightning and turbulence as a Boeing 777 flew over Taiwan through Typhoon Podul last night. The aircraft landed safely.

2,825,371 просмотров

Imagine being a passenger on the left side of the aircraft with a much better view of the runway than the pilot.

Imagine being a passenger on the left side of the aircraft with a much better view of the runway than the pilot.

3,029,552 просмотров

Videos

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The preliminary NTSB report on the United Airlines Flight 169 incident at Newark has been released. According to investigators, the crew encountered gusty headwinds and moderate turbulence on final approach to Runway 29. The captain disconnected the autopilot and autothrottles at about 880 feet and reduced thrust after the aircraft accelerated in the headwind. As the aircraft descended below 500 feet, the first officer repeatedly warned that the jet was becoming "slow" and later "still slow and a little low." Despite the decreasing airspeed, the approach continued and the captain responded to the automated 500-foot callout with "stable." Just seconds before touchdown, multiple crew members heard a loud "thump." After landing, the aircraft taxied normally to the gate, where the captain discovered significant damage to the aft fuselage. Investigators found three punctures, dents, and creases along the lower left rear fuselage. The damage was substantial enough to affect all three elements of the fuselage structure. The No. 1 left main landing gear tire also showed slash marks. The report also details damage to the truck involved in the collision, including windshield damage and punctures in the trailer's aluminum siding. Following the incident, United issued new operational guidance to pilots, warning against "ducking under" electronic or visual glide paths during the visual segment of an approach—a technique identified through its Safety Management System as contributing to dangerously low approach altitudes. The investigation remains ongoing.

Turbine Traveller

499,208 просмотров • 2 дней назад

This is the moment Frontier Airlines Airbus A321neo flight 4345 to LAX struck a pedestrian on Runway 17L during the takeoff roll at Denver.
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AMERICAN AIRLINES FLIGHT 191 — THE DAY THE DC-10 CHANGED AVIATION FOREVER 49 years ago today, May 25, 1979, American Airlines Flight 191 crashed moments after takeoff from Chicago O’Hare, killing all 271 people on board and 2 on the ground. It remains the deadliest single-aircraft crash in U.S. history. The McDonnell Douglas DC-10 had just rotated off Runway 32R when the unthinkable happened: the entire No.1 left engine and pylon tore away from the wing, flipped over the aircraft, and slammed onto the runway. The separation severed critical hydraulic and electrical systems, causing the left wing’s leading-edge slats to retract unexpectedly. With the right wing still producing full lift and thrust, the aircraft became catastrophically unbalanced. The left wing stalled first. Within seconds, the DC-10 rolled violently to a 112° bank angle, nearly inverted, before crashing into a field near a trailer park at the end of the runway. Investigators later discovered the root cause was improper maintenance procedures. To save time, the engine and pylon had been removed together using a forklift instead of following McDonnell Douglas’ approved method. The process damaged the pylon structure, creating cracks that went unnoticed until catastrophic failure occurred during takeoff. Even more tragic: simulator tests later proved the crew did almost everything correctly. Critical stall warning systems had been disabled by the electrical failure, leaving the pilots with no indication the left wing was stalling. Flight 191 reshaped aviation safety forever, leading to stricter maintenance oversight, redesigned inspection procedures, and independent stall warning systems for both pilots. A tragedy that changed aviation history forever. Video shows recreation footage.

Turbine Traveller

675,751 просмотров • 12 дней назад

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The MD-11 has always had a critical design flaw. It was manageable until someone screwed up. To improve fuel efficiency and range, its horizontal stabilizer was made smaller than those of earlier DC-10 variants. While the design delivered performance benefits, it also reduced the aircraft's natural pitch stability, particularly at slower speeds during approach and landing. To help compensate, the MD-11 relied heavily on computerized stability augmentation systems. Many crews also preferred flying slightly faster approaches, which improved pitch stability but could make the aircraft more challenging to manage during touchdown due to its weight and sensitivity in roll and yaw. These characteristics became evident in several high-profile accidents. In 1997, a FedEx MD-11 arriving at Newark was reportedly operating under the belief that runway length was limited, prompting the crew to aim for an immediate touchdown. The aircraft landed hard, bounced, and became unstable. Instead of executing a go-around, attempts to salvage the landing resulted in another severe impact, collapsing the landing gear and destroying the aircraft in a post-crash fire. All five crew members survived. The accident highlighted a key lesson: when an MD-11 bounced significantly after touchdown, a go-around was often the safest option. That lesson resurfaced in tragic fashion in 2009 at Narita, Japan. During strong and gusty crosswinds, a FedEx MD-11 touched down hard and bounced. Believing the aircraft could still be recovered onto the runway, the crew attempted to continue the landing. The resulting control inputs led to an even harder impact, loss of control, and a crash that destroyed the aircraft and claimed the lives of both pilots. 📹: buybygb

Turbine Traveller

205,691 просмотров • 5 дней назад

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How Ryanair saves money.

Turbine Traveller

5,157,417 просмотров • 3 месяцев назад

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Well that could have gone a lot worse.

Turbine Traveller

724,972 просмотров • 26 дней назад